摘要
To solve the conflict between stage-matching and computational cost during the 3-D(three-dimensional) aerodynamic optimization of multi-stage axial compressor, an optimization strategy was proposed, in which the stage to be optimized was simulated instead of the whole multi-stage compressor, while the stage environment was taken into account in the boundary conditions. The 4th stator with suction separation of a highly loaded 7-stage axial compressor has been optimized. Within the limited time, the adiabatic efficiency was improved about 0.8%, the total pressure ratio was improved about 4%, and the overall performance of the compressor was improved effectively. It is proved that the stage-matching and computational cost aer well balanced by this optimization strategy.
| 源语言 | 英语 |
|---|---|
| 页(从-至) | 1826-1831 |
| 页数 | 6 |
| 期刊 | Hangkong Dongli Xuebao/Journal of Aerospace Power |
| 卷 | 27 |
| 期 | 8 |
| 出版状态 | 已出版 - 8月 2012 |
指纹
探究 'Three-dimensional aerodynamic optimization of intermediate stator of 7-stage axial compressor' 的科研主题。它们共同构成独一无二的指纹。引用此
- APA
- Author
- BIBTEX
- Harvard
- Standard
- RIS
- Vancouver