TY - GEN
T1 - EXPERIMENTAL STUDY on DIFFERENT TIP CLEARANCE of LOW-SPEED AXIAL FAN
AU - Zhang, Ming
AU - Li, Jia
AU - Dong, Xu
AU - Sun, Dakun
AU - Sun, Xiaofeng
N1 - Publisher Copyright:
© 2021 by ASME.
PY - 2021
Y1 - 2021
N2 - Tip clearance flow is not only the source of undesirable noise but also a potential indicator for critical operating conditions with rotating stall or surge. It can induce blade vibration, which would cause premature blade failure when the vibration is strong enough. The paper presents experimental studies on the effects of tip clearance on the stall inception process in a low-speed high-load single stage fan with different tip clearance. From the point of view of flow range, it has been proved by computations that there is an optimal gap value, and an explanation is given according to different stall mechanisms of large and small tip clearance. However, the experiment of no tip clearance is not easy to achieve. In this experiment, a wearable soft wall casing was used to achieve "zero clearance", and an explicit conclusion was obtained. The pressure rise and efficiency are improved at small tip clearance. Instantaneous Casing Pressure Field Measurement was carried out: instantaneous casing pressure fields were measured by 9 high response pressure transducers mounted on the casing wall. At the near stall point with large tip clearance, a narrow band increase of the amplitudes in the frequency spectrum at roughly half of the blade passing frequency can be observed according to the spectrum of static pressure at points on the endwall near the leading-edge and above the rotor. This phenomenon was explained from two aspects: tip clearance flow structure and pressure signal spectrum.
AB - Tip clearance flow is not only the source of undesirable noise but also a potential indicator for critical operating conditions with rotating stall or surge. It can induce blade vibration, which would cause premature blade failure when the vibration is strong enough. The paper presents experimental studies on the effects of tip clearance on the stall inception process in a low-speed high-load single stage fan with different tip clearance. From the point of view of flow range, it has been proved by computations that there is an optimal gap value, and an explanation is given according to different stall mechanisms of large and small tip clearance. However, the experiment of no tip clearance is not easy to achieve. In this experiment, a wearable soft wall casing was used to achieve "zero clearance", and an explicit conclusion was obtained. The pressure rise and efficiency are improved at small tip clearance. Instantaneous Casing Pressure Field Measurement was carried out: instantaneous casing pressure fields were measured by 9 high response pressure transducers mounted on the casing wall. At the near stall point with large tip clearance, a narrow band increase of the amplitudes in the frequency spectrum at roughly half of the blade passing frequency can be observed according to the spectrum of static pressure at points on the endwall near the leading-edge and above the rotor. This phenomenon was explained from two aspects: tip clearance flow structure and pressure signal spectrum.
KW - Tip clearance
KW - stall
KW - unsteady flow
UR - https://www.scopus.com/pages/publications/85115443781
U2 - 10.1115/GT2021-59899
DO - 10.1115/GT2021-59899
M3 - 会议稿件
AN - SCOPUS:85115443781
T3 - Proceedings of the ASME Turbo Expo
BT - Turbomachinery - Axial Flow Fan and Compressor Aerodynamics
PB - American Society of Mechanical Engineers (ASME)
T2 - ASME Turbo Expo 2021: Turbomachinery Technical Conference and Exposition, GT 2021
Y2 - 7 June 2021 through 11 June 2021
ER -