15:1气氧/煤油变推力火箭发动机设计及试验

Translated title of the contribution: Design and Test of 15:1 GO2/Kerosene Variable-Thrust Rocket Engine
  • Yu Shu Jin
  • , Xu Xu*
  • , Shao Hua Zhu
  • , Liang Xiang
  • *Corresponding author for this work

Research output: Contribution to journalArticlepeer-review

Abstract

In order to improve the thrust adjustment level,broaden the use of propellant,enhance the control ability of thrust rocket engine,a GO2/kerosene variable-thrust rocket engine based on mechanical positioning dual-modulation scheme was designed by using theoretical calculations and ground test methods. The performance of variable-thrust engine and pintle injector,as well as the adjusting effect of mechanical positioning dual-modulation scheme were studied. The results show GO2/kerosene variable thrust rocket engine achieves stable combustion at 0.26~4.35MPa and generates 57.30~864.70N of thrust. Thrust variation ratio is 15. The maximum combustion efficiency is 97.14%. Besides,the flow control valve can accurately adjust the propellant flow and the pintle injector can actively control the injection pressure drop. Mechanical positioning dual-modulation scheme achieves the desired purpose. The variable thrust rocket engine shows the advantages of the mechanical positioning dual-modulation scheme in the application of the deep variable-thrust technology.

Translated title of the contributionDesign and Test of 15:1 GO2/Kerosene Variable-Thrust Rocket Engine
Original languageChinese (Traditional)
Pages (from-to)2438-2445
Number of pages8
JournalTuijin Jishu/Journal of Propulsion Technology
Volume39
Issue number11
DOIs
StatePublished - 1 Nov 2018

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